So after a very long and first ever multirotor build, my Tarot 650sport quadcopter it decides to crash for no apparent reason.
I was flying most of the day just fine, no problems whatsoever with the quad itself. The h3 3d gimbal on the other hand is another story. After 40+ minutes of flying (with a battery change in between) I let it hover for a bit. Then all of a sudden with no warning the thing just decides to flip. It's like the props on one side (couldn't tell if it was left or right) just went to max throttle or something. So here is my circumstance along with the equipment I was using.
1. I was flying at a glider field so there were at least 3 or 4 others but we were all spread out several hundred yards. In fact, I couldn't even see most of the operators because they were on the other side of a hill. But I could see their planes / copters. Could I have gotten interference from another pilot?
2. My h3 3d gimbal that I had just installed was acting up all day and was constantly twitching when the copter was running but worked great when it was stationary. ie no twitching when copter was on the ground and I moved the copter around to see the gimbal work.
3. Equipment
- Naza V2
-2.4ghz data link
-bluetooth ( I think the bt on my phone was still running becasue I had made some changes on the copters gains and forgot to turn it off)
-iosd mini
1. I was flying at a glider field so there were at least 3 or 4 others but we were all spread out several hundred yards. In fact, I couldn't even see most of the operators because they were on the other side of a hill. But I could see their planes / copters. Could I have gotten interference from another pilot?
2. My h3 3d gimbal that I had just installed was acting up all day and was constantly twitching when the copter was running but worked great when it was stationary. ie no twitching when copter was on the ground and I moved the copter around to see the gimbal work.
3. Equipment
- Naza V2
-2.4ghz data link
-bluetooth ( I think the bt on my phone was still running becasue I had made some changes on the copters gains and forgot to turn it off)
-iosd mini