I posted earlier, but I'm reposting with some video that shows what's going on. Really hoping to smooth this copter out and eventually use for aerial photography. Anyone have any ideas as to why this thing is so jumpy?
http://youtu.be/YjvYnAfvSzM
Here is the list of things I've done already - balanced multirotor, balanced props, reinforced crappy rctimer booms, calibrated ESC's to radio, used remote gains to try to find sweet spot.
http://youtu.be/YjvYnAfvSzM
Here is the list of things I've done already - balanced multirotor, balanced props, reinforced crappy rctimer booms, calibrated ESC's to radio, used remote gains to try to find sweet spot.