MadAtTheSky
Member
Hey guys,
I recently did a rebuild of a pre existing quad I have to condense some of the wiring and make the quad a little neater. I also added a brushless gimbal and upgraded the motors from Turnigy NTM 28-30's to Emax 3510's. The quad uses Naza M lite FC w/ GPS. I recalibrated everything there is to recalibrate.
During the test flight, the quad would randomly jump a foot in altitude and/or bank to the left or then to the right. It would do this randomly while I was trying to hover. The motors are connected directly to the ESCs without bullet connectors.
I went to a smaller prop and that made the erratic behavior less frequent but did occur after I started to yaw a bit and give more input.
Any help is GREATLY appreciated. Thanks!
I recently did a rebuild of a pre existing quad I have to condense some of the wiring and make the quad a little neater. I also added a brushless gimbal and upgraded the motors from Turnigy NTM 28-30's to Emax 3510's. The quad uses Naza M lite FC w/ GPS. I recalibrated everything there is to recalibrate.
During the test flight, the quad would randomly jump a foot in altitude and/or bank to the left or then to the right. It would do this randomly while I was trying to hover. The motors are connected directly to the ESCs without bullet connectors.
I went to a smaller prop and that made the erratic behavior less frequent but did occur after I started to yaw a bit and give more input.
Any help is GREATLY appreciated. Thanks!