Hi
Just completed a new 550 build (3d Printed). I have used brand new Naza V2, 4 RCX ESC 40A from myrcmart (http://www.myrcmart.com/rcx-40ahv-h...d-for-multicopter-simonk-firmware-p-6442.html) , 4 motors (http://www.myrcmart.com/rcx-be28149...ticopter-free-mounts-high-quality-p-6488.html)
Problem :
- In Manual mode, throttle variation drive a direct variation of speed, as expected and from 0% to 100% in a linear manner. All motors are in sync.
- In attitude or GPS, motor speed variation is not linear to throttle variation and kind of questionable... if I compare to my other hovership...
- Starting at throttle 0%...
- Initiate the motor and they turn at contsant idle speed... until I reach 50% throttle
- at 50% throttlle, the speed increase in an important gap... after which variation become linear with thgrottle variation...
- now the main problem is when reducing throttle... all fine until I reach 50%... but then below 50% the motors do not reduce speed at all. I can be 40,30,20,10% at throttlle the speed does not reduce.
I have not calibrated the esc (i used similar RCX even if smaller with a Naza M lite and had no issue) . So it may be an option.
My understanding is that at 50%, the quad shiouzld be hovering and keeping same altitude... so how do you land.,,. if reducing throttle does not reduce speed of motors...
just to add :
- I had a already a first crash due to a fly away... which indicated something strange,,, I had left the BEC on ESC back to DJI (my error). I basically stayed on ground until 50% and then it went at a very high speed, porjecting itse.f in the air... no choice than going back to manual as reducing throtttle would make no difference,. I manual I managed to get it back and crashed... as it was really tensed...
- Once again in manual I hear variation proper all along and this behave like my other quad in attitude mode.
- My other quad does not behave like this in attitude and whilst 50% keeps it hovering I can reduce throttle below 50% and speed reduces
So I am suspecting a compatibility issue between components or perhaps the calibration.. but then manual would not work ?
IDEAS WELCONE
Just completed a new 550 build (3d Printed). I have used brand new Naza V2, 4 RCX ESC 40A from myrcmart (http://www.myrcmart.com/rcx-40ahv-h...d-for-multicopter-simonk-firmware-p-6442.html) , 4 motors (http://www.myrcmart.com/rcx-be28149...ticopter-free-mounts-high-quality-p-6488.html)
Problem :
- In Manual mode, throttle variation drive a direct variation of speed, as expected and from 0% to 100% in a linear manner. All motors are in sync.
- In attitude or GPS, motor speed variation is not linear to throttle variation and kind of questionable... if I compare to my other hovership...
- Starting at throttle 0%...
- Initiate the motor and they turn at contsant idle speed... until I reach 50% throttle
- at 50% throttlle, the speed increase in an important gap... after which variation become linear with thgrottle variation...
- now the main problem is when reducing throttle... all fine until I reach 50%... but then below 50% the motors do not reduce speed at all. I can be 40,30,20,10% at throttlle the speed does not reduce.
I have not calibrated the esc (i used similar RCX even if smaller with a Naza M lite and had no issue) . So it may be an option.
My understanding is that at 50%, the quad shiouzld be hovering and keeping same altitude... so how do you land.,,. if reducing throttle does not reduce speed of motors...
just to add :
- I had a already a first crash due to a fly away... which indicated something strange,,, I had left the BEC on ESC back to DJI (my error). I basically stayed on ground until 50% and then it went at a very high speed, porjecting itse.f in the air... no choice than going back to manual as reducing throtttle would make no difference,. I manual I managed to get it back and crashed... as it was really tensed...
- Once again in manual I hear variation proper all along and this behave like my other quad in attitude mode.
- My other quad does not behave like this in attitude and whilst 50% keeps it hovering I can reduce throttle below 50% and speed reduces
So I am suspecting a compatibility issue between components or perhaps the calibration.. but then manual would not work ?
IDEAS WELCONE