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    Controllable RGB LEDS with taranis on multirotor ARDUINO

    Hey guys, i made a pretty cool rig, constisting of an arduino, some circuitry and some leds. the basic function is that i use right slider on taranis to change the brightness of LEDs, and a 3 position switch to change the actual colour that im changing the brightness of, look at the video, i...
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    hexacopter help

    Yep, they are, could unbalanced props really cause the problem?
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    hexacopter help

    I'm using the taranis x9d and looking at the channel monitor, yaw changes only changes yaw channel. I'm using the x8r SBUS port to send info, and when I click on naza, I choose DBUS as its the only option that works.
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    hexacopter help

    i have been studying for my specialist and method test! year 12 aint easy haha! ok another question and somewhat unrelated, its my 18th birthday soon, and, well, i want an oscilloscope. what should i be looking at? 500 seems a good price. thank again!
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    hexacopter help

    sorry for late reply, went out and bought the new escs, did what i had to do to get em running, and the multi rotor takes off just fine. roll, throttle and pitch work great, but yaw immediately induces roll and pitch, ultimately resolving to nothing but difficulty and well, a crash. do you think...
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    hexacopter help

    i have come to the conclusion that the problem is with my escs. Afro 30A escs work on 1000Hz refresh rate, and the naza v2 outputs 400Hz probably gonna buy a new set of escs, anyone care to comment before i do so? thanks
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    hexacopter help

    hey, jfro, i have done all of these things, multiple times and it doesnt seem to solve the problem, thank you for your input though, ill keep it in storage for a later date! motopreserve, yes, i did the esc callibration, all with a large array of jumpers to do them all at once. i am going to...
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    hexacopter help

    Hey, thanks for replying. The naza was on a blackout Mini h and it worked relatively good, put it on tarot 680, changed it to hexacopter mode, turned voltage protection off, set gains to approximately 120% and attempted to fly. Regarding your second question, I would throttle up in manual...
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    hexacopter help

    Hey guys, i have a home built Tarot 680 (hexacopter) with turnigy multistar 750kv motors and afro 30A escs, with naza v2 flight controller. there is something wrong, i cant seem to get it to fly correctly. i have exhausted all options that i currently know. the flight controller works perfectly...
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