Ok, it seems like the 2 front motors aren't spinning as fast as they should :-\
Even when I do the motor test on the assistant software - the 2 front propellers don't spin as fast as the rear ones.
Sorry... I've now got the gimbal working! However, whenever I try and take off it's just instantly nose diving - the front 2 propellers don't seem to be responding correctly. Whenever I try and switch the Receiver Type to PPM, there's no response either. Everything is recognised when set to...
Javier, thank you for your response! I understand that that's what I need to do, but literally how do I do this? Forgive me, but an 'idiots guide' step by step explanation would be greatly appreciated!!
Sorry, I'm having the same problem here...
"• Complete the X1 channel calibration then reduce the level of X1 after calibration"
I've done the calibration, but how do you reduce the level of X1 after calibration? Any help would be greatly appreciated!!