I tested my setup this evening and my quad flipped and crashed again. My setup incorporates 6s battery, Tiger MN3515 with Tiger motors Air 40A, 5V secondary power from a BEC to one of the Main Ports on the pixhawk and it still crashed. When I checked the logs my Roll and DisRoll were not...
Yes. I am using Tiger motors MN3515. Would you says that once you added the 5v to the main ports on the pixhawk, you stopped experiencing sync issues? I am really hoping this solves my problem or else I would have to go back to Esc with Bec.
Thank you very much f
Thank you very much. I will test my setup today and confirm. I am not using the KDE ESCs, I am using the new Tiger Motors Air T40A NO BEC with 6s lipo batteries. I think and believe I have been having sync issues which causes the drone to just flip in mid air within a...